Advertisement

We need your help now

Support from readers like you keeps The Journal open.

You are visiting us because we have something you value. Independent, unbiased news that tells the truth. Advertising revenue goes some way to support our mission, but this year it has not been enough.

If you've seen value in our reporting, please contribute what you can, so we can continue to produce accurate and meaningful journalism. For everyone who needs it.

View at Carnsore Point in Co Wexford. Google Streetview

Plane that crashed on Wexford beach lost engine power after appearing to suffer from fuel loss

The pilot and three passengers narrowly escaped death after the light aircraft made an emergency landing in September.

AN AIRCRAFT WHICH crashed on a Co Wexford beach two months ago appeared to suffer a sudden loss of fuel shortly before both engines cut out, according to a preliminary report into the accident.

The pilot and three passengers narrowly escaped death after the light aircraft made an emergency landing on Carnsore Beach, Co Wexford on 23 September when both engines stopped a few minutes apart as a gauge indicated there was a sudden, abnormal loss of fuel.

However, a preliminary report by the Air Accident Investigation Unit found no leaks in either tank.

The report also revealed that one engine on the same aircraft stopped after it experienced a sudden loss of 130 litres of fuel in ten minute while on a flight from France to Ireland five days earlier.

The AAIU said there was no evidence of a fuel leak in either engine, while a loose connection which caused the problem during the flight between Rennes and Waterford on 18 September was found to be secure.

As a result of the landing on Carnsore Beach, the pilot and one passenger sustained serious injuries and were airlifted to hospital by Irish Coast Guard helicopters that attended the scene.

The two other passengers were transported to hospital by ambulance for treatment for their injuries.

The AAIU said the pilot reported an abnormal drop in fuel levels as the aircraft was beginning an extended leg of a scheduled flight off the south coast, after which the right engine stopped.

Four minute later, the pilot said the gauge indicated there was no more fuel in the right engine at a time he believed there was sufficient fuel for around another 105 minutes flying time.

The French–registered aircraft, a Partenavia P68, with a group of researchers from University College Cork on board had left Waterford airport to record sightings of various marine wildlife.

The plan for the flight was to fly at low altitude along 16 predefined survey lines – each about 45km – along the south coast between Tramore and Carnsore Point.

When the planned survey was completed, the pilot determined that the remaining fuel would allow another one hour and 45 minutes of flying time and the group decided to conduct two more survey lines before returning to Waterford Airport.

The stopping of the right engine occurred shortly after the aircraft began the additional survey line.

As fuel levels in the left engine appeared stable, the pilot said he decided to return to Waterford Airport which was approximately 20 minutes flying time away.

However, he reported having difficulty in maintaining altitude on one engine and he did not believe it was delivering full power.

The pilot told AAIU investigators that he then decided to fly close to the shore in case he needed to make a forced landing.

Loose shale on the beach caused the plane to decelerate rapidly on touchdown which caused the aircraft to pitch down on its nose.

Significant structural damage was caused to the cockpit and forward cabin areas.

The report also revealed that the left engine spontaneously restarted and accelerated to full power immediately after landing.

The pilot exited the aircraft through the windscreen which had broken on impact, while the passengers exited by the door.

AAIU investigators noted the fuel tanks were filled prior to the flight with 74 litres of fuel recovered from the aircraft following the crash which would have allowed for over an hour’s flying time based on the pilot’s calculations.

The report noted that the pilot had carried out regular safety drills and briefings before each flight, while they had also completed a course of training for exiting an aircraft underwater at the National Maritime College of Ireland.

The AAIU said the investigation into the cause of the crash remained ongoing and a full report would be published in due course.

Readers like you are keeping these stories free for everyone...
A mix of advertising and supporting contributions helps keep paywalls away from valuable information like this article. Over 5,000 readers like you have already stepped up and support us with a monthly payment or a once-off donation.

Close
7 Comments
This is YOUR comments community. Stay civil, stay constructive, stay on topic. Please familiarise yourself with our comments policy here before taking part.
Leave a Comment
    Submit a report
    Please help us understand how this comment violates our community guidelines.
    Thank you for the feedback
    Your feedback has been sent to our team for review.

    Leave a commentcancel

     
    JournalTv
    News in 60 seconds